Hardinge Cataract 4-Jaw Chuck Repaired

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  • čas přidán 4. 04. 2024
  • Fixing this chuck was a major effort but I'm please with the end result. The chuck was made my Skinner but I think it's the original pre-1906 chuck for this lathe.

Komentáře • 94

  • @leslieaustin151
    @leslieaustin151 Před 3 měsíci +7

    Like it, you should! That was a great job on what I would have assumed to be a scrap chuck. Thanks for another great video. Your workshop is certainly a place to see wonderful ‘resurrections’. Thank you. Les in UK 🇬🇧

  • @AmateurRedneckWorkshop
    @AmateurRedneckWorkshop Před 3 měsíci +3

    Like I love to say where there is a will there is a way. Thanks for the video keep on keeping on.

    • @WinkysWorkshop
      @WinkysWorkshop  Před 3 měsíci

      Yep.... I had some issues with Will but he came around.

  • @billybike57
    @billybike57 Před 3 měsíci +3

    I just enjoy watching you restore old machine shop equipment, thanks for sharing!

    • @WinkysWorkshop
      @WinkysWorkshop  Před 3 měsíci

      Great.... I think watching would have been much easier, Ha

  • @jerryhill681
    @jerryhill681 Před 3 měsíci +2

    Congratulations on a very elegent solution to a difficult problem.

  • @TheAyrCaveShop
    @TheAyrCaveShop Před 3 měsíci +3

    Wow that was quit the repair job Mark, good you were able to save that old classic chuck..
    Well Done 👍👍

    • @WinkysWorkshop
      @WinkysWorkshop  Před 3 měsíci +1

      Thanks 👍 I agree, it looks goof on the Hardinge

  • @Bob_Adkins
    @Bob_Adkins Před 3 měsíci

    Another interesting and well-done repair on vintage machines!

  • @mdlanor5414
    @mdlanor5414 Před 2 měsíci

    All that really matters is if you are satisfied. You did an excellent job at repairing the now usable 4 jaw independent Metal Lathe Chuck.

  • @alanjackson4397
    @alanjackson4397 Před 3 měsíci +2

    Now that is a gutsy undertaking I’m not sure I would have tried

    • @WinkysWorkshop
      @WinkysWorkshop  Před 3 měsíci +2

      I thought about it for several weeks and it was a bit intimidating but then I thought... nothing lost if I fail, the chuck was not usable.

  • @mftmachining
    @mftmachining Před 3 měsíci +2

    Excellent repair, Mark. An unusual approach, never seen before. Congrats on yer success. An get yourself a precision ground bar, around 3/4 in. They pay for themselves in a month, only around 20 to 40 bucks. Simple tool with a lot of good uses.

    • @WinkysWorkshop
      @WinkysWorkshop  Před 3 měsíci +2

      Thanks! I have a linear rail bar about 3/4" but I misplaced it. I'll probably grind the inner jaws at some point but I'm please with the outcome as is.

  • @trollforge
    @trollforge Před 3 měsíci +2

    Maybe it;s just my OCD, but I would have had to go back and re-groove those circular lines on the face... Great job Mark!

  • @lv_woodturner3899
    @lv_woodturner3899 Před 3 měsíci +2

    Well done. As you said, a whole lot of work. Good that you saved this vintage chuck from the scrap bin. The inserts are stronger than the original cast ribs.
    Dave.

    • @WinkysWorkshop
      @WinkysWorkshop  Před 3 měsíci +1

      I'd say you are right about the strength. Thanks

  • @daviddazer2425
    @daviddazer2425 Před 2 měsíci

    I like it, too! It's always fascinating to see how you do things.

  • @magicbytes3835
    @magicbytes3835 Před 3 měsíci +1

    Hello Winky, wow your a real handy man, that was a brilliant idea that you adopted to repair that 4 jaw chuck, cheers from me. 😃👍👍👍👍👍

  • @rickpalechuk4411
    @rickpalechuk4411 Před 3 měsíci +1

    Trash to treasure. Nicely done Mark
    Cheers

  • @VanFlausch
    @VanFlausch Před 3 měsíci

    Nice Job, you did it again saving old metal with nice Ideas. Learning another thing^^

  • @lesmaybury793
    @lesmaybury793 Před 3 měsíci +1

    Wrll done, another innovative wothwhile rescue.

    • @WinkysWorkshop
      @WinkysWorkshop  Před 3 měsíci +1

      Thanks you, Might have easier to but a chuck but at least this one is probably original to the lathe.

  • @guye7763
    @guye7763 Před 3 měsíci

    I like it too, I was a bit skeptical at the start but I'm impressed. Well done!

    • @WinkysWorkshop
      @WinkysWorkshop  Před 3 měsíci

      Thanks.... I was a little afraid I'd go to all that work and a jaw would not fit.

  • @terrycannon570
    @terrycannon570 Před 3 měsíci +1

    Mark, I haven't seen a chuck that does not have the long end wobble with a piece that long. I just finished a project putting an E-Z view DRO on my old Clausing with magnets holding it in place. I revolt when I think of drilling and tapping into these old machines. As with most jobs I do it was 75% thought and 25% machining. Sequencing the work is imperative or else I machine myself into a corner. LOL Great job you have done in both thinking the job and machining the job.

    • @WinkysWorkshop
      @WinkysWorkshop  Před 3 měsíci

      Yeah... I try not to drill into the machines but sometimes you have to. I agree, I've never had a chuck clamp perfectly straight.

  • @MyMiniHomeWorkshop
    @MyMiniHomeWorkshop Před 3 měsíci

    There's that Necessity, Mother of Invention thing again, nice outcome. 👍

  • @mkegadgets4380
    @mkegadgets4380 Před 3 měsíci

    I think I would’ve shot the check out. But you saved it. Great job I never would’ve thought about that. Look forward to your next video.

    • @WinkysWorkshop
      @WinkysWorkshop  Před 3 měsíci

      Slotting might have worked well but attaching the steel to the chuck was the part that worried me.

  • @angelramos-2005
    @angelramos-2005 Před 3 měsíci

    Great fix,Mark.Thank you.

  • @Hoaxer51
    @Hoaxer51 Před 3 měsíci

    That had to feel a little weird running your cutter into your lathe chuck, I don’t know if my brain would let me do that! Lol
    That repair looks a touch busy, but in a good way, it matches that lathe perfectly. Thanks for sharing, you always come up with interesting videos that are fun watching.

    • @WinkysWorkshop
      @WinkysWorkshop  Před 3 měsíci +1

      Thanks 👍 Yep when the end mill hit the chuck there was no turning back!

  • @hpda44
    @hpda44 Před 3 měsíci

    Very good job! You are one heck of a craftsman.

  • @anthonycash4609
    @anthonycash4609 Před 3 měsíci

    Any thing that you can fix with tools you already have is always worth it. You've gained another tool to add to your arsenal with a little of your time and knowledge and always pushing yourself to at least try only adds to your abilities in the future. Good job Mark.

  • @neillawson4493
    @neillawson4493 Před 3 měsíci +1

    Having found the centre of the chuck using your DRO, you could then have used the Pitch Circle Diameter function to place all of the holes on the same diameter.

    • @WinkysWorkshop
      @WinkysWorkshop  Před 3 měsíci

      You are right. To be honest, I'm a little weak on the DRO

  • @adamlambert1307
    @adamlambert1307 Před 3 měsíci

    That is amazing! Great work!

  • @larry3064
    @larry3064 Před 3 měsíci

    Very well done. Looks great. Thanks for sharing

    • @WinkysWorkshop
      @WinkysWorkshop  Před 3 měsíci

      Thanks for watching! I'm happy with the outcome.

  • @jarihakli4343
    @jarihakli4343 Před 3 měsíci

    Wow, very innovative and nice work!

    • @WinkysWorkshop
      @WinkysWorkshop  Před 3 měsíci +1

      Thanks... yeah it was a LOT of work but in the end it worked well.

  • @rickknowlton5700
    @rickknowlton5700 Před 3 měsíci

    Nice fix to a tricky problem.

  • @joerogi8401
    @joerogi8401 Před 3 měsíci +1

    Woo hoo number 1, good morning Sir.

  • @MatthewTinker-au-pont-blanc
    @MatthewTinker-au-pont-blanc Před 2 měsíci

    Very nice fix! I would have brazed in and machined afterwards, but I think you way is better! Cheers, Matthew

    • @WinkysWorkshop
      @WinkysWorkshop  Před 2 měsíci

      Thanks, I was afraid I would get some of the braze under the key (slide) where I could not machine it off.

  • @MR-si1eq
    @MR-si1eq Před 2 měsíci

    Good morning Winky from Cave City. 😊

  • @txrascal
    @txrascal Před 3 měsíci

    Nice work!

  • @dans_Learning_Curve
    @dans_Learning_Curve Před 3 měsíci

    Excellent!

  • @t.d.mich.7064
    @t.d.mich.7064 Před 3 měsíci

    Hey, good fix. When setting up a rotary table, I found that it works well to set the rotary table dial on "0", clamp the table to the mill table and tram the rotary table parallel to the mill table. Then Tram the center hole in the table to the spindle, setting X,Y,"0" on the DRO. Then after all that, then mount your work piece and tram the work piece to the mill spindle at DRO "O"

    • @WinkysWorkshop
      @WinkysWorkshop  Před 3 měsíci

      I started to do that but the mounting slots and the bolt holes on the chuck were not in line to do that. Thanks

  • @chipperkeithmgb
    @chipperkeithmgb Před 3 měsíci +1

    Great job from oxford England 🏴󠁧󠁢󠁥󠁮󠁧󠁿

    • @lesmaybury793
      @lesmaybury793 Před 3 měsíci

      And from here in Leighton Buzzard 🇬🇧 🏴󠁧󠁢󠁥󠁮󠁧󠁿

    • @WinkysWorkshop
      @WinkysWorkshop  Před 3 měsíci +1

      Isn't the internet amazing? Thanks

    • @WinkysWorkshop
      @WinkysWorkshop  Před 3 měsíci +1

      Very good to hear from you, thanks

    • @lesmaybury793
      @lesmaybury793 Před 3 měsíci

      @@WinkysWorkshop it beats semaphore 😁

    • @leslieaustin151
      @leslieaustin151 Před 3 měsíci +1

      @@lesmaybury793 yup, the English fog gets in the way…. But Morse works🤣

  • @alanremington8500
    @alanremington8500 Před 3 měsíci

    Good job !!

  • @dcraft1234
    @dcraft1234 Před 3 měsíci

    Turned out pretty good! I think I would have bored that center out with an endmill in the rotab to at least knock the corners off.

    • @WinkysWorkshop
      @WinkysWorkshop  Před 3 měsíci

      Yeah.... I used to worry about interrupted cuts but so far its never been a problem. This cut really smoothly. Thanks

  • @bombardier3qtrlbpsi
    @bombardier3qtrlbpsi Před 3 měsíci

    Nice job 👍

  • @65cj55
    @65cj55 Před 3 měsíci

    Good Fix Winky.

  • @kennethomeara9848
    @kennethomeara9848 Před 3 měsíci

    I bet that was kind of nerve-wracking, but great job!

    • @WinkysWorkshop
      @WinkysWorkshop  Před 3 měsíci

      Yeah... I was more worried about wasting a lot of time and effort. A new chuck would be easy and not super high priced for one that small.

  • @robertwalker7457
    @robertwalker7457 Před 3 měsíci

    Mate, this is a great effort. I am not sure that I would be game to do myself? Might grinding the jaws help?

    • @WinkysWorkshop
      @WinkysWorkshop  Před 3 měsíci

      I probably will grind the jaws... yes it was a lot of work.

  •  Před 2 měsíci

    Did you haunt eBay looking for a replacement chuck? I have good luck there getting stuff for my two South Bends but maybe that is a different world.

    • @WinkysWorkshop
      @WinkysWorkshop  Před 2 měsíci

      That would have been a lot less work. I'm sure I could have found something. The thing is, a lot of the available chucks ar very deep meaning they the end of the jaws are farther away from the lathe bearings. This might have been okay but its not a good thing on lathes with smaller spindles.

  • @howardosborne8647
    @howardosborne8647 Před 3 měsíci

    That worked out nicely👌
    The split in the socket end of the jaw screw is a common fault on 4 jaw independent chuck screws. The most common cause is that the screws are through hardened and not tempered on the outer socket end hence they are vulnerable to splitting due to the chuck key 'springing' the screw socket head.
    Pratt Burnerd 4 jaws are notorious for this problem.
    If you check out Alan Enot's channel (Enots Engineering) you will find a video where he made a new set of jaw screws which work just fine.
    Link to Enots Engineering video on new chuck jaw screws here: czcams.com/video/F0mChMn7zXw/video.htmlsi=T8uq9pC5j4gLkVpd

    • @WinkysWorkshop
      @WinkysWorkshop  Před 3 měsíci

      Thanks, making new screws is fairly extreme. I'll watch the video but I thin I'll try to repair mine