How to Nice 3000+ control shaft leaning

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  • čas přidán 24. 08. 2024

Komentáře • 13

  • @asad6437
    @asad6437 Před 2 lety +1

    Good vedio 💓💓

  • @mahmoudmady2798
    @mahmoudmady2798 Před 2 lety

    السلام عليكم بجي عطل 35 ازاي ترتيب مفناطيسات البير ؟

    • @MasudOfficialkwt
      @MasudOfficialkwt  Před rokem

      Err 35 occurred before the
      run contactor pick-up
      1 .check whether the 1st
      down forced deceleration
      is valid
      2 .F4-01=1
      3 .whether the inspection switch on the inspection state and able to done the inspection run 4 .F0-00=1
      Err 35 occurred as soon as the run contactor pick-up
      1 .check whether the inspection switch on the inspection state Err 35 occurred during running
      1 .check whether running overtime, , run over the time of Err 35 occurred when meet the 1st levelling
      position 1 .Whether the F4-03
      INCREASE WHEN UP, DECREASE WHEN
      DOEN, switch the main board PGA and PGB if it is not . 2 .Level sensor N .O, N .C .setting error . 3 .level sensor signal flash, check the plate Err 35 during running: 1 .check whether run overtime of F9-02 setting value, and no receiving of
      levelling signal
      2 .the floor distance less than 50cm, check the sensor 3 .the F6-00 setting too small
      Run to the top floor: 1 .the 1st
      forced slowdown is valid and juadge on the door-area, check whether the learned floor amount are same as the setting of
      F6-00 and F6-01 . 2 .Error occurs if the lifting
      height less than 50cm Err35 occures when power-on
      Check whether the plate
      length is 0 after power-on

  • @tauhidalislam3799
    @tauhidalislam3799 Před 3 lety +1

    Please talk and explain. Sir

    • @MasudOfficialkwt
      @MasudOfficialkwt  Před 3 lety +1

      what's you need to know telling me

    • @tauhidalislam3799
      @tauhidalislam3799 Před 2 lety

      I want to know how to start inspection run and control wring.? Please explain step by step.sir.

    • @tauhidalislam3799
      @tauhidalislam3799 Před 2 lety

      Gearless and geared.

    • @MasudOfficialkwt
      @MasudOfficialkwt  Před 2 lety +4

      Group F0: Basic parameters
      F0-00 Control mode
      0: Sensorless vector control
      (SVC)
      1: Closed-loop vector control
      (CLVC)
      2: Voltage/Frequency (V/F) control
      1 - ★ 192
      F0-01 Command source
      selection
      0: Operation panel control
      1: Distance control
      1 - ★ 192
      F0-02
      Running speed under
      operation panel
      control
      0.050 to F0-04 0.050 m/s ☆ 193
      F0-03 Maximum running
      speed 0.250 to F0-04 1.600 m/s ★ 193
      F0-04 Rated elevator speed 0.250-4.000 1.600 m/s ★ 193
      F0-05 Rated elevator load 300-9999 1000 kg ★ 194
      F0-06 Maximum frequency 20.00-99.00 50.00 Hz ★ 194
      F0-07 Carrier frequency 0.5-16.0 6.0 kHz ★ 194
      Group F1: Motor parameters
      F1-00 Encoder type
      0: SIN/COS encoder
      1: UVW encoder
      2: ABZ incremental encoder
      3: ECN413/1313 absolute
      encoder
      0 - ★ 195
      F1-01 Rated motor power 0.7-75.0 Model
      dependent kW ★ 195
      F1-02 Rated motor voltage 0-600 Model
      dependent V ★ 195
      F1-03 Rated motor current 0.00-655.00 Model
      dependent A ★ 195
      F1-04 Rated motor
      frequency 0.00-99.00 Model
      dependent Hz ★ 195
      F1-05 Rated motor speed 0-3000 Model
      dependent RPM ★ 195
      F1-06 Encoder initial angle
      (synchronous motor) 0.0-359.9 0 Degree
      (°) ★ 196
      F1-07
      Encoder angle
      at power-off
      (synchronous motor)
      0.0-359.9 0 Degree
      (°) ★ 196
      F1-08 Synchronous motor
      wiring mode 0-15

    • @tauhidalislam3799
      @tauhidalislam3799 Před 2 lety

      Saalam aliykum sir, thanks. Plz make video all errors solution with your voice.

  • @sergeim5009
    @sergeim5009 Před 2 lety

    Help nice 3000 error 40 what to do?

  • @basitghayas1644
    @basitghayas1644 Před rokem

    How to remove Error 35 during shaft learning please tell me?

    • @MasudOfficialkwt
      @MasudOfficialkwt  Před rokem

      Err 35 occurred before the
      run contactor pick-up
      1 .check whether the 1st
      down forced deceleration
      is valid
      2 .F4-01=1
      3 .whether the inspection switch on the inspection state and able to done the inspection run 4 .F0-00=1
      Err 35 occurred as soon as the run contactor pick-up
      1 .check whether the inspection switch on the inspection state Err 35 occurred during running
      1 .check whether running overtime, , run over the time of Err 35 occurred when meet the 1st levelling
      position 1 .Whether the F4-03
      INCREASE WHEN UP, DECREASE WHEN
      DOEN, switch the main board PGA and PGB if it is not . 2 .Level sensor N .O, N .C .setting error . 3 .level sensor signal flash, check the plate Err 35 during running: 1 .check whether run overtime of F9-02 setting value, and no receiving of
      levelling signal
      2 .the floor distance less than 50cm, check the sensor 3 .the F6-00 setting too small
      Run to the top floor: 1 .the 1st
      forced slowdown is valid and juadge on the door-area, check whether the learned floor amount are same as the setting of
      F6-00 and F6-01 . 2 .Error occurs if the lifting
      height less than 50cm Err35 occures when power-on
      Check whether the plate
      length is 0 after power-on