Missing Back Gear Tooth. South Bend 13 (pt6)

Sdílet
Vložit
  • čas přidán 16. 06. 2022
  • When the back gear was engaged durring the small test drive I did prior to buying this machine, it made a slight knock per revolution of the chuck.
    I guessed then that the bull gear or cone gear had a damaged tooth, now is the time to see what I could do to fix it.
    Apart from a bit of a cockup I made when I started my first cut, the tooth would have been right on the money. OK… so I made a mistake by forgetting to check the milling machine was properly secured, but its done now. Lets see how long it lasts...
  • Jak na to + styl

Komentáře • 146

  • @debike3077
    @debike3077 Před 8 hodinami

    Very clever.👍

  • @joell439
    @joell439 Před rokem +5

    Absolutely phenomenal work (ignoring the whoopsie of course, but we are all only human). Can't believe after all these years of watching YT machining community videos that I have never stumbled upon your channel. I've immediately subscribed, toggled the bell on, and I am now anxiously looking forward to enjoying your entire portfolio of work. 👍👍😎👍👍

    • @Thesheddweller
      @Thesheddweller  Před rokem

      Hi, sorry i didn't reply, I missed your comment. But I thank you for your kind comments. Cheers

  • @billdavies6463
    @billdavies6463 Před 2 lety +4

    Paul, I'm very impressed by your use of the involute principle to progressively cut the profile. I've seen other methods - base circle and tapes or wires, calculating offsets and using a slitting saw - but this is a new method to me.

    • @Thesheddweller
      @Thesheddweller  Před 2 lety +1

      Hi Bill, I’ve said it so many times - there’s always more than one way to skin a rabbit. regards

  • @fna-wrightengineering
    @fna-wrightengineering Před 2 lety +7

    Great job on the repair, Paul. The method you used to index and cut the tooth is very clever! Looks like the gear should work a treat.
    (Don't sweat the witness mark... Gives it character!)

  • @slakjawnotsayin5451
    @slakjawnotsayin5451 Před 5 měsíci

    WOW!!! This is fantastic!

  • @tp8845
    @tp8845 Před 2 lety +1

    Great Job. This ist Dentist Work. Perfekt!

  • @michaelbritton9778
    @michaelbritton9778 Před 4 měsíci

    Lovely job.

  • @alanremington8500
    @alanremington8500 Před rokem

    Excellant repair !!

  • @captainraypaul4919
    @captainraypaul4919 Před 2 lety +1

    Don’t fret about the lill oopsy! It gives it character! good job on the fix, it should work great 👍🏻

    • @Thesheddweller
      @Thesheddweller  Před 2 lety +1

      Hi, I did wonder if zapping a little blob of weld on the top would fix it but I quit while I was ahead. cheers

  • @markamy357
    @markamy357 Před 2 lety

    As an owner of several old lathes I know missing teeth are quite common, this really looks like a very do able method of repair, thank you.

  • @joshwalker5605
    @joshwalker5605 Před 2 lety

    Always a pleasure to see a new video from you - thanks!

  • @2stroke1971
    @2stroke1971 Před 7 měsíci

    Nice! As I am going through my South Bend 744 9a, I have found 3 gears that need attention, the two back gears and the bull gear. The small back gear is a loss, so I will replace that, but the bull gear is missing 2 teeth and the larger back gear 1. Now I will fret over whether to try and find those as used parts or whether to try and repair those 3 teeth for about a week before I do anything. Awesome video as always!

    • @Thesheddweller
      @Thesheddweller  Před 7 měsíci

      Hi. Thanks for watching, one thing I will say about this method of repair is that the tooth is not a precise shape, but it still works well, albeit a little noisy until it’s worn in, then it’s as good as new. All the best.

  • @MrPhatNOB
    @MrPhatNOB Před 2 lety

    HAHA MUNTED! Love that word.
    Perfect repair though!! Oops and all.
    Very good technique to line up the cutter without using a dividing head or special tooling.
    This is why your channel is one of my few favourites!!

    • @Thesheddweller
      @Thesheddweller  Před 2 lety

      Hi, that phrase Munted is one I picked up in New Zealand, it sort of hits the mark nicely. cheers.

  • @FCleff
    @FCleff Před 2 lety

    Your creativity knows no bounds. Thanks for sharing.

  • @graedonmunro1793
    @graedonmunro1793 Před 2 lety

    really clever and good to watch

  • @Akitene
    @Akitene Před 2 lety

    Lessons were learned but such a good job! Simple and efficient.

  • @bkoholliston
    @bkoholliston Před 2 lety +2

    Fun to see your approach! I would have gone for bronze braze but yours is better. The way you setup that gear on the mill is brilliant!

    • @Thesheddweller
      @Thesheddweller  Před 2 lety +2

      Hi, my first thought was to go and see a cast iron welder when he told me it will be £250+ to weld up the tooth I had no choice but to use plan B. Cheers

  • @RB-yq7qv
    @RB-yq7qv Před 2 lety

    Very nicely done

  • @ab-shop
    @ab-shop Před rokem +1

    Ciao Paul, this is Alberto from AB-SHOP Italy !! Stopping by from Paul, of the Knackler's workshop !!! Wow, i have to say wow in front at this work: this is your first video that i watch and it is the first time that i see this type of repair without a dividing head: really a great job also with a nice and clear explanation too!! From today Paul you have a new subscriber to your channel, me !! A big Ciao from Italy Paul, Alberto.

    • @Thesheddweller
      @Thesheddweller  Před rokem +2

      Hi Paul. the gear works perfectly well, my next video ‘an update’ will show up a few more horrors though. regards.

  • @lito4u
    @lito4u Před rokem +1

    Beautiful work

  • @raikbusse7697
    @raikbusse7697 Před 2 lety

    A very clever way to repair a gear. Never seen like this before and can be done with seemingly little effort. I pay respect. Greetings from Germany, Raik

  • @andyknappenberger7512

    I zip-tied a spring to keep pressure up on the pin to disengage the back gear. Nothing sucks more than having a nice cut going and it just slows down and blows up an insert. On the other end of the spectrum, I have a bungie cord to keep the back gear engaged.

    • @Thesheddweller
      @Thesheddweller  Před rokem

      Hi, sorry i didn't reply, I missed your comment. Thank you I might even need to use that idea if I have problems. Cheers

  • @be007
    @be007 Před 2 lety

    thanks for the upload, another trick learned !

  • @vandalsgarage
    @vandalsgarage Před 14 dny

    When I do repairs like this, I'll frequently make copies of the repair part, so that I don't have to repeat the full operation if the repair fails. It would have been fairly simple to make two or three identical copies of the tooth blank while that setup was still on the milling machine, so that you had another blank ready to fit up into the gear body. Still, some very good ideas here, I have a similar repair needed on one of the gears in the headstock of my Cincinnati lathe.

  • @craigtate5930
    @craigtate5930 Před 2 lety +1

    love this approach. in the past I have had some success welding in a new tooth and using slitting saw and 60° AND 45° cutters to shape. I will definitely keep your techniques in mind for future repairs

    • @craigtate5930
      @craigtate5930 Před 2 lety

      i hope you get a chance to do a follow up video in the future to show how it holds up also

    • @Thesheddweller
      @Thesheddweller  Před 2 lety

      @@craigtate5930 Hi, the slitting saw process is pretty much the same thing. Regards

  • @DavoShed
    @DavoShed Před 4 měsíci

    Great video! I never would have thought of doing it like that.
    I especially liked your single point dovetail cutter.
    I destroyed a couple of change gears off my Atlas Lathe beyond repair so I found a involute cutter set on eBay.
    They were not very expensive and I made some new gears from scratch out of brass. Way better than the original zermak stuff.
    I have a rotary table I could tip up on its side to use as a dividing head.
    Slotted the key way using the quill on the mill like a slotted.
    Came out ok.
    Worked great.

  • @Dave.Wilson
    @Dave.Wilson Před 2 lety

    That was an ingenious repair Paul, you could call the cockup a makers mark. Would never thought of that myself, thanks for sharing.

  • @TheKnacklersWorkshop
    @TheKnacklersWorkshop Před 2 lety

    Hello Paul,
    Great stuff... I really like the logic you followed, it worked well. See you on the next one.
    Take care.
    Paul,,

    • @Thesheddweller
      @Thesheddweller  Před 2 lety +1

      Hi Paul. Thanks I think quite a few people are going to try this one. regards

  • @JamesP_TheShedShop
    @JamesP_TheShedShop Před 2 lety

    That is absolutely genius. Bravo.

  • @TheRecreationalMachinist

    Rustinox sent me. Great channel, and a great repair 👍 🇬🇧

  • @steved8038
    @steved8038 Před 2 lety

    So what's a small mistake between friends ! 😁Very well thought out and machined and very informative.Thank you for sharing.

  • @matts_shed
    @matts_shed Před 2 lety

    I love your videos thanks for sharing. The mistakes just remind us your human.

  • @nefariousyawn
    @nefariousyawn Před 2 lety

    Very clever. Thanks for sharing!

  • @hasanusman9809
    @hasanusman9809 Před 2 lety

    Very nice👍👍 work

  • @brucematthews6417
    @brucematthews6417 Před 2 lety +2

    First off I really enjoy the look, feel and pacing of your videos. There's a good serving of "meat" without a lot of "parsley" filler.
    Next is the wonderful analysis and thoughts on how to place and hold items. As any machinist knows it's not about the metal removed but the setup details before the power is turned on. You really hit the bell with the setup details on this one. I learned a bit more than usual from this video which I hope I can remember when the need comes up in my own shop. The "trapping" of the gear with the blocks engaging the lower teeth is brilliant. Matched by the way you picked off the flanks to mill the new tooth.
    Keep up the great work and I wish you many more subscribers. And yes, I think my stomach turned over as badly as yours when the tool took off sideways... A feeling only another machinist would understand I'm sure... .:D

    • @Thesheddweller
      @Thesheddweller  Před 2 lety +1

      Hi, Thanks, I’m glad you enjoyed the video, yes I’m surprised it didn’t bust the cutter too. Cheers

  • @steinmargunnarsson3709

    Interesting way of tooth repair; thumbs up

  • @Steviegtr52
    @Steviegtr52 Před 2 lety

    Hi Paul. Thanks for showing the method you used. Very good. Also for showing your mistake, which many would have covered up somehow.
    Regards.
    Steve.

  • @DK-vx1zc
    @DK-vx1zc Před 2 lety

    Excellent! very clever

  • @Klythia
    @Klythia Před 2 měsíci

    ΕΞΑΙΡΕΤΙΚΉ ΕΡΓΑΣΊΑ!!!

  • @ParsMaker
    @ParsMaker Před 2 lety

    Nice work

  • @tonyray91
    @tonyray91 Před 2 lety

    Niece repair Paul. Exactly how I saw my dad do it on a clock wheel only press fitted and filed to shape by hand.

    • @Thesheddweller
      @Thesheddweller  Před 2 lety

      Hi Tony, It just goes to prove that nothing in machine engineering is new. Regards

    • @tonyray91
      @tonyray91 Před 2 lety

      @@Thesheddweller Or sound engineering principles will stand the test of time.

  • @howder1951
    @howder1951 Před 2 lety

    Nice bit of work and really great technique. I have done a similar repair on a SouthBend, but tapped a few screws, brazed and filed to form. It is great to get it back into production. anyhow. enjoyed, cheers!

    • @Thesheddweller
      @Thesheddweller  Před 2 lety

      Hi, thanks. Cheers

    • @oliver90owner
      @oliver90owner Před 2 lety

      Agreed, a good job well done. I drill and tap for a couple of grub screws, then bolt on a couple of thin plates, fill with braze and recut the teeth with an involute gear cutter or home-profiled fly-cutter.
      One gear I had just had screws loctited in place and filed to shape. It never failed.

    • @Thesheddweller
      @Thesheddweller  Před 2 lety

      @@oliver90owner That sounds like a good idea.

  • @lecnac855
    @lecnac855 Před 2 lety

    Still a very good job and it works so I would call it a success .

  • @grahamshedd9225
    @grahamshedd9225 Před 2 lety

    Brilliant!

  • @markrainford1219
    @markrainford1219 Před 2 lety

    Clever solution.

  • @honeycuttracing
    @honeycuttracing Před 2 lety

    Great work sir, hate moving the wrong wheel or just slipping up and making a nice fix into not such a nice fix, but looks like you caught it quickly enough to avoid catastrophic damage, could have slaped some JB Weld in that divot on side of that tooth, stuff is strong 💪, thanks for showing us that no one is perfect and we all make mistakes 👍

  • @manusholm3536
    @manusholm3536 Před 2 lety

    i like your indexing system. will use it in fiture. had to coppy a gear that i couldnt get the tooth count in my rotary table without serious mucking about. ended had to buy one. could gave used your system and a nother gear as index wheel.....nect time.

  • @TheDistur
    @TheDistur Před 2 lety

    That's a nice repair even with the oops.

  • @alasdairhamilton1574
    @alasdairhamilton1574 Před 2 lety +1

    A bit more JB Weld on it and it will be fine.👍🏴󠁧󠁢󠁳󠁣󠁴󠁿

  • @therealspixycat
    @therealspixycat Před 2 lety

    Smart idea to align the tooth using two blocks!

  • @robertpearson8798
    @robertpearson8798 Před 2 lety

    Nice tooth repair, very incisive.

  • @chrisstephens6673
    @chrisstephens6673 Před 2 lety

    An intelligent and pragmatic approach, but i bet it will always irk you when you see it.😉

    • @Thesheddweller
      @Thesheddweller  Před 2 lety

      Hi, thanks, I will probably forget its there I’m old enough for that to happen,😁

  • @nacerdepie6255
    @nacerdepie6255 Před 3 měsíci

    Paulo, tu sabes que ese engranaje no quedo con la resistencia necesaria debido al error en el corte en la parte superior, hubiera sido más honesto de tu parte realizar nuevamente la reparación desde cero, hasta conseguir un resultado correcto y resistente. Saludos

  • @ScatManAust
    @ScatManAust Před 2 lety

    Very different approach and something I would never have thought of.
    Simply brilliant .
    Regarding the cockup , as you had made the tooth from steel, what about using a mig and slowly carefully build it up without putting too much heat to mess up the JB weld.
    And machine it again as before ?
    Just a thought

    • @Thesheddweller
      @Thesheddweller  Před 2 lety

      Hi, thanks, I had considered that very fix, but I’m not prepared to upset the apple cart so to speak. regards

  • @Rustinox
    @Rustinox Před 2 lety

    You're right, Paul. For these low speed geas it doesn't matter much if there is a little damnage on the tooth.

  • @simonpenny2564
    @simonpenny2564 Před 3 měsíci

    that is a great fix, realised with intelligent solutions given limited tools - kudos! I have the same problem - on a south bend back gear (10K in this case). I'm wondering how important the dovetail is, structurally - a square section would be so much easier ;) Also since there's no load on the top of the tooth, why would you not put the grub screw - or two in from the top? Did you consider brazing or silver soldering it in?

  • @samueltaylor4989
    @samueltaylor4989 Před rokem +1

    Bozo visited your shop I see!

  • @Raul28153
    @Raul28153 Před 2 lety

    Excellent dentristy~!! I wonder why you didn't braise the tooth in

    • @Thesheddweller
      @Thesheddweller  Před 2 lety +1

      Hi, The reason why I didn’t Braze it in is mainly due to the risk of cracking the gear. The tooth can only be brazed in or one built up using brazing rod if the whole casting is first heated to a given temperature, then using a concentrated quality flame like using Oxyacetylene to stroke the rod in. I haven’t got such equipment. I hope this goes a little way to explaining why I didn’t do it that way. Cheers

  • @stevengehm1287
    @stevengehm1287 Před 2 lety

    RightOn! (American for "FarOut"...)

  • @humanistwriting5477
    @humanistwriting5477 Před 2 lety

    Well using a dovetail to repair a gear Ina bull tooth is brilliant! If I had seen this technique 4 months or earlier I could have repaired a broken bull gear for my company and saved then 20,000 dollars us in lost contracts and a new parts I would have been a hero, as it stands the welder tried to weld in a new tooth and cracked the entire gear.
    oh well, next time I suppose!

  • @stevecanny1583
    @stevecanny1583 Před 2 lety

    Well done shed dweller! :)

  • @TalRohan
    @TalRohan Před 6 měsíci

    nice one.
    On the subject of the wandering cutter, no that the tooth is steel would it be possible to weld in the missing material and then machine it back again...just thinking out loud incase it had somehow made a mole hill out of a mountain
    fantastic series btw thanks for sharing

    • @Thesheddweller
      @Thesheddweller  Před 6 měsíci +1

      Hi, yes it would have been fairly easy to weld, but the heat could have affected the resin bond and I didn't want that. cheers.

    • @TalRohan
      @TalRohan Před 6 měsíci

      @@Thesheddweller that's a very good point , I suppose braising the tooth in. The first place might have worked but you still run the risk of melting it again if you weld.
      Thanks for sharing

  • @ogaugeclockwork4407
    @ogaugeclockwork4407 Před rokem

    Nice repair!!!

  • @pgiamel
    @pgiamel Před 2 lety

    I'm sorry you did a great job, but it wasn't easier and safer to refill with cast iron electrodes or better still with AISI 309, it has perfect adhesion with cast iron and is workable.
    What a huge job you did, congratulations

    • @Thesheddweller
      @Thesheddweller  Před 2 lety +1

      Hi, I don’t have a TIG welder and a nearby cast iron welding specialist was charging £250+ (€300+)to do the job for me. this was my safest and cheapest method, thanks for the info though. cheers

  • @yurycz8933
    @yurycz8933 Před 2 lety

    👍

  • @hobbyeubauer1162
    @hobbyeubauer1162 Před 2 lety

    Gear Dentist 😉👍

  • @mikemarriam
    @mikemarriam Před 2 lety

    If you had the broken off segment of tooth do you think it could have been brazed back on and operated successfully? Asking for a friend.

    • @Thesheddweller
      @Thesheddweller  Před 2 lety

      Hi, the problem is, getting it done professionally is very expensive. Brazing is possible provided the main cast component is heated beforehand to try and prevent the component cracking, but I’ve also heard many stories of complete failure. cheers.

  • @heybabycometobutthead
    @heybabycometobutthead Před 2 lety

    As the repair is mild steel, you can just fill the mistake with a blob of weld.

    • @Thesheddweller
      @Thesheddweller  Před 2 lety

      Hi, Its possible, and I did consider that, but I didn’t want to risk upsetting the apple cart. cheers

  • @NellsMechanicalManCave

    Brilliant method of indexing the gear teeth Paul. That out of the box thinking at its finest!
    Was Heath involved in this ? 🤔🤔🤔
    Cheers Nell

    • @Thesheddweller
      @Thesheddweller  Před 2 lety

      Hi Nell, well we sort of bounced a few ideas between each other his idea helped. A guy just the other side of town wanted £250+ just to weld it up. guess what, I’ve still got £250 quid in my pocket. cheers mate

    • @NellsMechanicalManCave
      @NellsMechanicalManCave Před 2 lety

      @@Thesheddweller what is he, a dentist? They charge those sort of rates 🤣

  • @TheModelmaker123
    @TheModelmaker123 Před 2 lety

    Given the tooth was mild steel could you have tig welded a repair on the tooth with minimal heat?

    • @Thesheddweller
      @Thesheddweller  Před 2 lety

      Hi, I can’t afford a TIG welder. cheers.

    • @TheModelmaker123
      @TheModelmaker123 Před 2 lety

      @@Thesheddweller a machine shop with out a welder?

    • @Thesheddweller
      @Thesheddweller  Před 2 lety

      @@TheModelmaker123 Hi, I have a welder, I don’t have a TIG welder.

  • @69uremum
    @69uremum Před 2 lety

    Never heard the term G clamp used before, are you sure you don't mean C clamp?